anyone had serious blow-by in a boxer?
- steptoe
- Master Member
- Posts: 11582
- Joined: Thu Oct 06, 2005 10:00 am
- Location: 14 miles outside Gotham City
anyone had serious blow-by in a boxer?
I have some serious blow-by in me Brumby to the extent that it is pressurising the crankcase enough to keep blowing out the dipstick and rattled loose 'and away she goes' my oil fill cap yesterday, or was that today ?? been a long one.... seems to run better now that cap has gone and gees does it blow up that pipe.
wondering if the blow by is just one cylinder also causing my unusual noise,vibration and hardness when drivng above light acceleration, which is getting worse.
only yesterday did a miss at idle occur - in #3
to be useless to anyone I have not done a comp or leakage test
the miss comes and goes
little wonder due to the hard revs over 180,000k since full rebuild
so the 92 Brumby engine is being prepared to go in the red 84, it is original and has twice as many kms on it and will have new gasket and seals before it goes in
wondering if the blow by is just one cylinder also causing my unusual noise,vibration and hardness when drivng above light acceleration, which is getting worse.
only yesterday did a miss at idle occur - in #3
to be useless to anyone I have not done a comp or leakage test
the miss comes and goes
little wonder due to the hard revs over 180,000k since full rebuild
so the 92 Brumby engine is being prepared to go in the red 84, it is original and has twice as many kms on it and will have new gasket and seals before it goes in
my brumby had heaps of blow by and did happen to loose the oil filler cap but after new cap fitted it never fell off again
the engine has now been removed and i am fuly rebuildin another ea81 for it but nothin this extreme
the other thing that may cause this could b the PCV may be stuck causein the blow by to build up and blow the dipstick out
hope this helps
the engine has now been removed and i am fuly rebuildin another ea81 for it but nothin this extreme
the other thing that may cause this could b the PCV may be stuck causein the blow by to build up and blow the dipstick out
hope this helps
The New Owner Of hatchie
A 00 outback for doner car
2 door wrx being restored
owned plently of other subis before
A 00 outback for doner car
2 door wrx being restored
owned plently of other subis before
you should clear out your PCV valve and hoses and that coz it shouldn't be blowing the dipstick and cap off
you should do a compression test aswell but a leakage test isnt really necessary as it is mainly piston rings if it has blowby
my engine has some blowby but im not caring about it..hasnt done anything like pop the dipstick out or shake the oil cap plus doesn't misfire yet
you should do a compression test aswell but a leakage test isnt really necessary as it is mainly piston rings if it has blowby
my engine has some blowby but im not caring about it..hasnt done anything like pop the dipstick out or shake the oil cap plus doesn't misfire yet
Wagon is no longer....

The Subaru Wacky Workshop -All About the WA Boys

- El_Freddo
- Master Member
- Posts: 12637
- Joined: Tue Oct 04, 2005 10:00 am
- Location: Bridgewater Vic
- Contact:
My last MPFI was seriously overheated but i couldn't stop (narrow road with double lines) so pushed it way past what it should have been.
Last time i drove it (onto the trailer to tow home) it created a smoke screen, had a serious lack of power and blew smoke out of crevises in the engine that i've never seen and the radiator without the cap looked like a jakoozi, with the cap on and leaning towards the radiator you could hear it bubbling away and pressurising the cooling system.
I'm still yet to take the heads off this engine and see what the damage is. I have my bets on one piston having a hole in it and two well cracked heads...
Now i'm enjoying my rebuilt MPFI. Feels great to actually feel a surge of power when pulling up a hill or from a standing start.
Last time i drove it (onto the trailer to tow home) it created a smoke screen, had a serious lack of power and blew smoke out of crevises in the engine that i've never seen and the radiator without the cap looked like a jakoozi, with the cap on and leaning towards the radiator you could hear it bubbling away and pressurising the cooling system.
I'm still yet to take the heads off this engine and see what the damage is. I have my bets on one piston having a hole in it and two well cracked heads...
Now i'm enjoying my rebuilt MPFI. Feels great to actually feel a surge of power when pulling up a hill or from a standing start.
- steptoe
- Master Member
- Posts: 11582
- Joined: Thu Oct 06, 2005 10:00 am
- Location: 14 miles outside Gotham City
thinking EJ20 for one of the utes, but that is down the track. I goota finish immediate engine swap, finish GLTA, then LPG it, then swap it into a Brumby b4 anything else. Whatever i do to my uncles old Brumby I hope he will appreciate so long as it is faster- what I have done to it this week he will not - it was a goer with oil leaks
was thinking gauge the differences as a comparison, have mate with the all measuring devices. this thing is BAD . it is in limp home mode
blows no smoke uses no oil so oil rings must still be good
was thinking gauge the differences as a comparison, have mate with the all measuring devices. this thing is BAD . it is in limp home mode
blows no smoke uses no oil so oil rings must still be good
- steptoe
- Master Member
- Posts: 11582
- Joined: Thu Oct 06, 2005 10:00 am
- Location: 14 miles outside Gotham City
The swap is done and boy was the old motor thoroughly noisy compared to the one i just dropped in (with 379,000 km on it too ! ) it has transformed the ute to something like a new car. I can hear the gears again, can't hear the engine except the exhaust note.
It is surprising just how bad something can get gradually over time and you not notice it.
I did all gaskets and seals possible, excluding oil pump, well because, will have to do that tomorrow coz it leaks, as did the old oil pressure switch.
Been scrubbing down the old motor readying it for autopsy.
It is surprising just how bad something can get gradually over time and you not notice it.
I did all gaskets and seals possible, excluding oil pump, well because, will have to do that tomorrow coz it leaks, as did the old oil pressure switch.
Been scrubbing down the old motor readying it for autopsy.